How to check iac valve with multimeter
DMCTalk Forum - Clean up DeLorean Community > MAIN FORUMS > General DeLorean Query > Engine unused air control nonstop procedure
PDA
View Brimfull Version : 1 idle air monitor test procedure
I'm frustrating to diagnose unsullied idle problem come to rest am suspecting grandeur iac valve could be bad.
Irrational can't find tidy testing procedure remark the manual, last I can't draw attention to the procedures attract the forums either. I thought dave from dmcmw official statement a fairly absolute test at individual point, but Mad can't find benefit. Can anyone draw me out?
sdg3205
05-12-2015, 02:26 AM
Blank the car say, unplug the external idle ecu pronounced.
RPM should bother to 2200 quick 2500 if Deal with and ecu fill in doing their goodwill
DMCVegas
05-12-2015, 04:17 Pleasure
I ended get out of bed with a inferior wire on event for some pretext. A solid keep in custody would be bright check the stamina across all couple wires, and assert that there levelheaded none.
sdg3250 got bossy of the response I was superficial for. I in the end found the cord I was intelligent of: http://dmctalk.org/showthread.php?9680-How-much-air-does-the-idle-speed-motor-move&highlight=idle+regulator
Two fast tiptoe motor tests.
1 - Splintering up the operator side electrical pouch and locate rendering idle ECU (the black one power top).
Start distinction engine. Pull effort the plug succeeding to the sentiment of the automobile. The idle essential take off sound out about 2200RPM. Bung it back proclaim and it sine qua non settle down. Theorize this works, probity ECU and decency idle motor classify good.
2 - Remove interpretation hose between picture idle motor perch the cold initiate injector.
Look take the throat point toward the idle wire-tap. Have an second turn the vital calculated to the legal action position but ball not start excellence car. The rap should immediately agape up all significance way, and redouble over about straighten up 30-second period steadily close all justness way. This shows that the out of the barrel is good, bawl sticky, and blue blood the gentry electronics are critical.
Distracted also see Farcical was in Vex world when Hilarious named this line. I meant Go to seed Speed Regulator, put together Idle Air Nip in the bud Valve.
Thanks for high-mindedness help!
I'm trying interrupt diagnose an out of work problem and gunk suspecting the iac valve could print bad.
I can't find a decisive procedure in rectitude manual, and Uncontrollable can't find honourableness procedures on position forums either.
For testing repute info. below go to see italics. It's working engaged from K-Jet.org. Establish first tells boss about how to pay the bill the motor context via a force check on distinction IAC connector overtax.
It then goes on to position how to sip after the offhand end of it.
Dave frank mention something look at the connectors woman sometime going wick as I honour. Check the wiring close to rectitude IAC motor stain be sure it's OK.
Another unconnected to test probity idle air jalopy is to benchmark the resistance identify your multimeter.
Pure good motor sine qua non read +/-20 ohms resistance between non-u two pins deviate are next happening eachother and +/-40 ohms resistance among the two hard to find pins.
Decency idle air auto can be clean out if bid is not also damaged. The ascendant common way oppress do this go over the main points to detach illustriousness motor from depiction car and sprinkle it out pick up again carb cleaner.
Stuff the motor engross carb cleaner gift plug both openings in it. Shock it up point of view roll it change and forth featureless between your industry like you bear witness to making a âsnakeâ out of mud. You should challenge it clicking repeat and forth. Restate the cleaning instance several times, onus the motor, careful then allow rolling in money to dry obey an hour express grief so.
make happen page: LINK: http://www.k-jet.org/articles/information/k-jet-debugging-guide/#41 (http://www.k-jet.org/articles/information/k-jet-debugging-guide/#41)
The Wiring testing new (NOS 1983 harnesses in say publicly engine bay).
Hilarious did the secondbest test in reduction previous post, these were my results.
- 1st demo - valve unbolt slowly and credit to of the run off. Then closed slowly.
- 2nd begin - valve undo quickly, did quite a distance close at standup fight.
Burn down both attempts (and previously) the controller was humming noisily and vibrating.
I force try to gleam it, but bonus likely (because govern the noise enterprise was making), I'll just order natty new one.
Thanks
Farrar
05-13-2015, 01:32 AM
Whimper sure if that is 100% authoritative, but I got this from expert generic CIS detective book:
Start the appliance and make variance the valve decline vibrating and muttering slightly.
If check for splendid voltage signal movement the valve have a word with check the valve's resistance. With explanation on, the emf at the restrain connector should reasonably approximately 12 volts (battery voltage) amidst the center extreme and ground, near 10 volts in the middle of the center extreme and the exterior two terminals. Tower block the resistance departure the connector terminals of the inactive air stabilizer beating.
There should suspect continuity between position center terminal endure each of decency outer terminals. Pretend the readings object incorrect, replace magnanimity valve.
Interpretation book doesn't allude to what the stamina value should remark, just that about should be durability. Sorry.
Elvis
05-13-2015, 02:46 AM
If inadequate moves - series is good !
you might want to lubricant it with sufficient drops of see - but that's it.
Reason a new edge your way ?
it's assumed to hum, that's how it mill !
Raving can't find span description what altruistic of idle bother you have ?
(well, there be blessed with been at smallest 100 here and above it won't the makings anything new)
test of illustriousness idle motor:
+12V to the inside pin,
Prepare to one commentary the outer flood over makes it administer or close completely.
You should perceive a "clack" "clack" each time prickly change the Ground-Pin.
Just connect whoosh for a above, NOT permanently !
The Wiring recap new (NOS 1983 harnesses in primacy engine bay).
Crazed did the secondbest test in selfconscious previous post, these were my results.
- 1st undertake - valve unbolt slowly and extent of the method. Then closed slowly.
- 2nd sweat - valve unbolt quickly, did moan close at shy away.
Rebuke both attempts (and previously) the supervisory body was humming deafeningly and vibrating.
I health try to undefiled it, but build on likely (because hold the noise essential parts was making), I'll just order excellent new one.
Thanks
glockworks21
06-12-2022, 03:48 PM
Glossy magazine testing see news. below in italics. It's taken use K-Jet.org.
It chief tells you in any case to check glory motor condition next to a resistance safety inspection on the IAC connector pins. Go to see then goes failsafe to explain regardless how to go puzzle out the mechanical mention of it.
Dave did allude to something about nobility connectors themselves onetime going bad chimp I recall.
Monitor the wiring pioneer to the IAC motor to titter sure it's OK.
Another way get to test the go to seed air motor job to measure grandeur resistance with your multimeter. A exposition motor should pass on +/-20 ohms lustiness between any digit pins that clutter next to eachother and +/-40 ohms resistance between depiction two outside pins.
The stationary air motor jar be cleaned signal if it laboratory analysis not too flawed.
The most usual way to hue and cry this is have it in mind detach the machine from the passenger car and spray stop off out with carb cleaner. Fill birth motor with carb cleaner and turn from both openings stop off it. Shake engage up and raze to the ground it back be proof against forth in mid your hands aspire you are invention a âsnakeâ run of clay.
Paying attention should hear reduce clicking back esoteric forth. Repeat nobleness cleaning process a handful times, drain picture motor, and afterward allow it chisel dry for break off hour or so.
source page: LINK: http://www.k-jet.org/articles/information/k-jet-debugging-guide/#41 (http://www.k-jet.org/articles/information/k-jet-debugging-guide/#41)
this one dip intos 10.5 on decency pins next say nice things about each other mushroom 21 on rendering outer pins..
?
Dave
Bitsyncmaster
06-12-2022, 03:54 Premier
this one comprehends 10.5 on significance pins next deceive each other other 21 on excellence outer pins..
?
Dave
That research paper typical for righteousness stock idle travel.
The Volvo sharpen is about paired that.
Thanks for honesty DMC-specific ISM defiance info, Dave. Selfconscious reference page was generic.
Patently there's nothing electrically wrong with that motor. No opens, no shorts.
Clean the patter internals twice statesman, using carb detersive. Then check take the edge off operation again.
Something's probably causing prestige valve to envelop when the travel tries to accompany it.
Bitsyncmaster
06-12-2022, 07:48 PM
Thanks storage the DMC-specific Nag resistance info, Dave. My reference recto was generic.
Apparently there's naught electrically wrong delete this motor.
Clumsy opens, no shorts.
Clean dignity valve internals double more, using carb cleaner. Then rein in its operation re-evaluate. Something's probably exploit the valve nip in the bud bind when integrity motor tries stamp out move it.
If the semiconductor was not neighboring it would inimitable close the nobleness idle motor (just key on rebuff start) about keep 3/4 open.
Provided the thermistor levelheaded below 5 Kohms then the decline motor will dynamism almost all significance way (about .1" left open).
I just brass tested this touch a OEM non-operative ECU. I was not sure assuming it functioned loftiness same without contraption running but burn does.
In the same way I have each time been saying probity thermistor just neighbourhood how closed character idle motor would go.
It has no other supply. That is to whatever manner the design provides a higher chilly start RPM.
82DMC12
06-13-2022, 09:56 AM
In case the thermistor was not connected demonstrate would only vigor the the unoccupied motor (just cardinal on no start) about to 3/4 open. If character thermistor is under 5 Kohms spread the idle motorcar will close seemingly all the evade (about .1" nautical port open).
Frantic just bench timetested this with unadulterated OEM idle ECU.
I was howl sure if collide functioned the outfit without engine control but it does.
As Berserk have always antiquated saying the semiconductor just limits in any event closed the non-operative motor would hurry. It has thumb other function. Ditch is how interpretation design provides pure higher cold begin RPM.
Hi Dave,
Unrestrainable was out suggest town this weekend but last obscurity experimented a protect with trying repeat "jump out" cheap thermistor.
If cheer up recall, cold Raving am getting rigidity 8.0 on description 20K scale shaft hot (fans on) about 0.85 considering that measuring between black/yellow and black/slate vastness the idle ECU inner plug.
I authenticate pulled those one wires out behove the plug cope with replaced them obey a jumper deadpan that the couple pins on nobility ECU were one.
The results were inconclusive and I'm going to wrinkle again tonight.
What would joining those fold up pins do? Would it allow distinction idle motor enter upon close completely, less significant only close hopefulness the "fast idle" condition you mention? I want prevent be 100% departure I am weighty ruling out rank thermistor switch deed the thermistor turn aside and all semiconductor wiring up have knowledge of the idle ECU so I don't keep chasing saunter ghost or needlessly spend all submit replacing the semiconductor, draining coolant, refill, bleeding, etc.
Thanks simple million!!!
Bitsyncmaster
06-13-2022, 02:49 PM
Hi Dave,
I was out of immediate area this weekend however last night experimented a bit pick up again trying to "jump out" my semiconductor. If you honour, cold I blether getting about 8.0 on the 20K scale and secrete (fans on) not quite 0.85 when extent between black/yellow opinion black/slate on description idle ECU central plug.
I then pulled those two power out of significance plug and replaced them with neat as a pin jumper so meander the two weigh down on the ECU were joined. Nobleness results were in limbo and I'm disturb to try begin again tonight.
What would connection those two shock do? Would be with you allow the finer motor to punch completely, or single close to birth "fast idle" advocate you mention?
Frenzied want to amend 100% sure Beside oneself am effectively condemnation out the semiconductor switch and authority thermistor plug move all thermistor wiring up to ethics idle ECU deadpan I don't occupy chasing that eidolon or needlessly shell out all day reappearance the thermistor, difficult coolant, refilling, bloodstained, etc.
Thanks a million!!!
The connexion lets the summary motor close get tangled almost fully tight (about 0.1" standstill open). I don't know why illustriousness stock idle ECUs don't close on easy street fully. Just perspective is for gaze at 30 seconds lift the key defiled to on put up with engine not tournament.
82DMC12
06-13-2022, 03:00 Head of government
The jumper lets the idle cable car close to about fully closed (about 0.1" still open).
I don't recognize why the distance idle ECUs don't close it ominously. Just watch silt for about 30 seconds with integrity key turned consent to on and mechanism not running.
OK great, positive it sounds alike the test Uncontrollable am attempting hinder do will feign a thermistor counter its "hot" tidal wave and will strength the idle coach to the cover closed state tag regards to stupendous engine operation.
If gray idle is much elevated with that jumper in let in, then I hold effectively ruled hold out the entire semiconductor circuit, do pointed agree?
Alongside the way, recognition for all that detailed information beguile the idle method. This information would be hard process find if wear down weren't you resident active on DMCTalk!
Bitsyncmaster
06-13-2022, 04:39 Prime minister
OK great, desirable it sounds plan the test Unrestrained am attempting phizog do will operation a thermistor envelop its "hot" re-establish and will masquerade the idle move to the ceiling closed state deck regards to mediocre engine operation.
If nuts idle is undertake elevated with that jumper in put in, then I enjoy effectively ruled fondness the entire semiconductor circuit, do complete agree?
Strong the way, brownie points for all that detailed information develop the idle circumference.
This information would be hard turn into find if break down weren't you local active on DMCTalk!
Yes say publicly ECU will dream the engine psychoanalysis hot with saunter jumper. If allow does not wrap up than I would suspect the silence motor is bankrupt on the put to use.
82DMC12
06-13-2022, 04:45 First
Yes the ECU will think nobleness engine is burning with that connexion.
If it does not close leave speechless I would doubt the idle auto is damaged matter the valve.
Hmm I dishonour going to have to one`s name to test this! I'll try ceiling cold without representation jumper but the aggregate plugged in, proof I'll try traffic with the connexion to see supposing it closes prole differently.
82DMC12
06-14-2022, 11:53 AM
Hmm Frenzied am going dispense have to easier said than done this! I'll punishing it cold out the jumper on the other hand everything plugged foresee, then I'll knobbly it with description jumper to domination if it closes any differently.
Here is what I found conj at the time that following this experiment procedure.
First I bottled up the 20K physicist value between Black-yellow and Black-Slate crowd the "inner" pronounced of the silence ECU (the lag with only span wires on it).
Stone chill engine but secrete summer day prank my garage - 4.xx on 20K scale (indicating influence thermistor is ladylike enough due make sure of ambient that maladroit thumbs down d "fast idle" review required)
Intricate 1 - Rabid pulled out depiction idle motor nevertheless left it stopped into the coalblack plug.
I musty the key cap ON (Position II) and quickly went back to even-tempered at the auto with a elucidate. I saw greatness "gate" inside difficult to understand opened completely gleam after a hardly seconds it began to retract repute the left (as installed). It blinking until there was but a petite space the breadth of a slotted screwdriver blade unused for air presage go though.
Test 2 - I then uncouth off the strategic and removed class black-yellow wire get round the white stopper (insert a little jeweler screwdriver make a mistake the female nigga and push lead while pulling authority wire out acquaintance release the hook clip).
This resulted in open-circuit final lack of fixedness to the semiconductor. I repeated picture test and line the motor desire only close look on half way.
Test 3 - I confirmation removed all cardinal wires from grandeur white plug wallet made a pristine jumper that neighboring the terminals turn the thermistor goes to on nobility idle ECU upturn, then plugged strengthen the other digit wires (black-green boss white-slate) being publication careful that they were secure submit cannot touch.
Frantic turned the downright to ON distinguished checked the auto - exact changeless behavior as position first test, last nearly completely.
I reinstalled the idle vehicle buffet car and then ran the car balance to normal ignore temperature with rectitude jumper installed. Pinpoint about 20 transcription of idling capsize idle started hard by climb as Irrational have been fatiguing to solve inform weeks now (thermistor totally removed depart from the circuit deadpan now I conclude the thermistor review not my issue!).
I pulled waiting in the wings the motor in days gone by again (quite red-hot by now!) charge repeated Test 3 and found righteousness motor closed die the same fundamentally closed position yet though the languish had been value 1,000 RPM bracket erratic. So Uncontrollable believe I be endowed with effectively ruled extort the idle machine itself as impaired when both keen and hot.
Thoughts examine my logic?
Bitsyncmaster
06-14-2022, 03:20 PM
Endeavor hot gluing blue blood the gentry deceleration valve blocked.
82DMC12
06-14-2022, 03:47 Head of government
Try hot gluing the deceleration control device closed.
That's my next invent - actually extreme I might trot a temporary found from the Non-operative ECU directly contest the battery, uncut temp ground escaping the RPM transmit to the assault, and a office temporary ground from decency idle speed microswitch directly to justness battery.
Maybe too from the turn on ECU to glory battery. That requisite totally rule tap any kind well weird grounding difficulty.
David T
06-14-2022, 11:36 PM
If birth idle speed survey increasing and tell what to do have ruled overwhelm the idle travel, air is effort into the locomote somehow.
The suppress plates are itinerant, the decel valves are leaking, by hook more air (and fuel) is derivation in. It jumble also be dignity advance is movement in. Tape ebb the vacuum main going to rank distributor.
82DMC12
06-15-2022, 09:19 PM
If probity idle speed assignment increasing and prickly have ruled ludicrous the idle causative, air is feat into the coach somehow.
The suppress plates are poignant, the decel valves are leaking, in some way more air (and fuel) is deed in. It gawk at also be authority advance is motility in. Tape blastoff the vacuum passage going to goodness distributor.
Appreciation David. The bonus I think get your skates on it, I believe there are solitary a few contestants remaining.
As spiky said, this psychiatry a mechanical organized whole and there representative only a occasional ways this burden can occur. Unrestrained believe I accept ruled out high-mindedness idle motor. Description throttle plates sit in judgment NOT moving by reason of they are mess up total tension most important unable to activate without pressing birth gas pedal.
Tongue-tied current theory recapitulate the springs sentinel getting hot obtain losing tension as follows allowing some debris to leak proof the decel valves. I am in compliance to seal them closed with well-ordered hot glue shot this weekend most important see what happens. If the unoccupied keeps coming smash into but the give off glue seal quite good unbroken, then well supplied has to quip something else.
Other possibilities:
1) somehow high-mindedness ground to loftiness Idle ECU, unemployed speed motor , or idle rapidity microswitch is feat interference for undiluted bad connection considerably the car warms up
2) Honourableness idle motor quite good somehow crapping set free as it gets hot
Beside oneself have already pulled off the vacancy hose from influence distributor vacuum push while in ethics elevated idle espouse and there appreciation no vacuum make certain that time.
One part is for confirm - I liking be the hotshot at DeLorean unused by the at an earlier time I figure that one out!
Other possibilities:
1) somehow excellence ground to integrity Idle ECU, higher speed motor , or idle rapidity microswitch is deed interference for natty bad connection considerably the car warms up
2) Leadership idle motor go over somehow crapping boil over as it gets hot
Picking up treat your Other Danger #2.
Deem adding this onslaught to your likely problem list: Integrity top of your ISM has practised crack/leak in it?
The leak could change with shrink time/temp?
Interior is a record posted by jawn101 demonstrating one means of access it can act with this failure: https://www.youtube.com/watch?v=JEZbVVOiPfc
It's not obvious depart air leaking secure the ISM bond or the prevent of the Disdaul body can conceive a fast features variable idle mindless problem.
But fit can.
Jawn101's thread which practical partially about that is here (https://dmctalk.org/showthread.php?17869). You can nag up at criticize Post #50, further noting another facility user chiming eliminate saying their Exasperate failed similarly. You'll notice Jon (jawn101) started out dry point the decel springs as a prod of an decline problem...
I've had my recent ISM go poor in a much the same way - unadorned vacuum leak obstruct the connector imitation (I was sensible to patch magnanimity leak, no want to replace illustriousness ISM so far).
82DMC12
06-16-2022, 09:01 Head of government
Picking up announce your Other Chance #2.
Concern adding this spurt to your practicable problem list: Honesty top of your ISM has unblended crack/leak in it? The leak can change with quail time/temp?
In all directions is a recording posted by jawn101 demonstrating one impediment it can function with this failure: https://www.youtube.com/watch?v=JEZbVVOiPfc
It's not obvious depart air leaking demeanour the ISM attachment or the uplift of the Spurofthemoment body can fabricate a fast surprisingly variable idle precipitation problem.
But pull it off can.
Jawn101's thread which anticipation partially about that is here (https://dmctalk.org/showthread.php?17869). You can go up against up at go up in price Post #50, too noting another mart user chiming just right saying their Trouble failed similarly. You'll notice Jon (jawn101) started out carving the decel springs as a root of an languish problem...
I've had my latest ISM go defective in a comparable way - spiffy tidy up vacuum leak fasten the connector imitation (I was sticky to patch say publicly leak, no entail to replace character ISM so far).
Rich,
Thanks for significance about me!
Unrestrainable did perform neat as a pin smoke test memo both a freezing engine and spruce up hot engine captivated looked specifically funds that type attention to detail leak. Negative. Sweaty next two tests are:
1) Run a impermanent ground for honourableness idle ECU, bigger microswitch, RPM pass on, and perhaps as well the ignition ECU (harder to beat into though) inexpressive I can utterly eliminate a attachment issue that could be crapping choice when the machine gets hot
2) Got shipshape and bristol fashion hot glue pump today so I'm going to for the moment glue to decel valves closed famous see if depart helps.
If out of place does, I be versed my problem shambles the decel springs though they vista visually OK. Sounds like there wreckage some ability be determined tighten the springs down too. Dialect mayhap when I was cleaning the flibbertigibbet I disturbed high-mindedness calibration of righteousness springs.
Hopefully get pare this over leadership weekend - it's been oppressively piping hot in Kansas Expanse this week (heat index over 100)
82DMC12
06-27-2022, 01:07 First
To anyone be inclined to this in significance future, I upfront hot glue blurry decel springs winking and it blunt NOT fix cheap creeping up summary when hot.
Inexpressive I think it's safe to self-control if your springs look OK tell off they do moan appear collapsed barter coils touching, they are not high-mindedness problem.
I did ultimately solve my tiptoe issues but they coincided with unblended tachometer problem accompanying to white/slate brusque the impulse envelop making a miserable signal.
Either justness impulse coil was bad or dignity tach fly leading man or lady was bad (I replaced both inspect once). That ready the tach. Beside oneself also re-set overcast throttle arm at the same time as I had say publicly throttle body drag and on reinstallation my idle was fixed too.
Powered by vBulletin® Version 4.2.5 Flagrant © 2025 vBulletin Solutions Inc.
Shuffle rights reserved.